The upgradation of methane in biogas by hydrogenation of CO has been currently recognized as a promising route for efficient full utilization of renewable biogas with potential benefits for storage of renewable hydrogen energy and abatement of greenhouse gas emission. As a main constituent of biogas, CO can act as a backbone for the formation of additional CH by hydrogenation, then producing higher amounts of biomethane. In this work, the upgradation process was investigated in a prototype reactor of double pass operation with vertical alignment using an optimized Ni-Ce/Al-MCM-41 catalyst. The experimental results show that the double pass operation that removes water vapor during the run can significantly increase CO conversion, resulting in higher CH production yield. As a result, the purity of biomethane increased by 15% higher than a single pass operation. In addition, search for optimum condition of the process was carried out within an investigated range of conditions including flowrate (77-1108 ml min), pressure (1 atm-20 bar), and temperature (200-500 °C). The durability test for 458 h was performed using the obtained optimum condition, and it shows that the optimized catalyst can perform excellent stability with negligible influence by the observed change in catalyst properties. The comprehensive characterization on physicochemical properties of fresh and spent catalysts was performed, and the results were discussed.

Download full-text PDF

Source
http://www.ncbi.nlm.nih.gov/pmc/articles/PMC10250424PMC
http://dx.doi.org/10.1038/s41598-023-36425-5DOI Listing

Publication Analysis

Top Keywords

pass operation
16
double pass
12
upgradation methane
8
methane biogas
8
biogas hydrogenation
8
prototype reactor
8
reactor double
8
optimized ni-ce/al-mcm-41
8
ni-ce/al-mcm-41 catalyst
8
optimum condition
8

Similar Publications

Want AI Summaries of new PubMed Abstracts delivered to your In-box?

Enter search terms and have AI summaries delivered each week - change queries or unsubscribe any time!